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I got a chance to get back to the annual today. I warmed up the engine with a quick flight. Tossed the cowl and plenum off, grabbed my compression tester only to find I couldn't rotate the valve. The grease in it seemed to of solidified somewhat making it difficult to turn. Disassembly was quick and after a quick lube it works better than new. Compression tests turned out great, all above 75! Did a wobble test on all intake and exhaust valves. By the end of this long day, I completed nearly every inspection for the FWF. Took the plugs, mag and K&N filter home to work on them in a more comfortable environment.
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Last Modified: October 5, 2024 |